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Site contents © D. Bailey 2001-2011 |
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K&WVR Winter Steam
Gala
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Added 14th Feb 2011
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A
lack of steam to record seems to be a feature of the early months
of the year but the drought ended for me on 11th February 2011, the
first day of the Keighley & Worth Valley Railway's steam gala
with the prospect of two Black 5s to record.
A forecast of dry, calm but dull weather proved accurate for once
and provided excellent recording conditions as I found when I reached
Keighley shortly before 11 o'clock and I went to my usual 'weekday'
recording spot just outside Keighley station.

The need for different weekday and weekend recording spots is easy
to explain; on weekdays the adjacent builder's merchant and a nearby
warehouse are often in full swing with wagons and fork lift trucks
heading here and there so the spot I use has a good solid wall screening
me from most of the noise. At times when these enterprises are closed,
a better spot becomes a possibility at the other side of the line
but on this Friday morning that wasn't an option.
The first train I could record was hauled by one of the visiting
Black 5s; this was the unique Stephenson link motion example, 44767
which appropriately carries the name 'George Stephenson'.
It's been quite a few years since I last heard this loco and I recall
it being quite loud. I'm glad to report that it still is, as you can
hear as it takes 6 coaches out of Keighley.
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44767 departing from Keighley |
4:42
2.15MB
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The L&Y 0-6-0 957 took the next train
out of Keighley.
This was a shuttle to Ingrow and 957 had two magnificently restored
L&Y coaches to haul along with the Jinty tagged on at the rear.
47279 was making its final gala appearance before coming out of service
for overhaul.
As 957 departs, the other visiting Black 5, Ian Riley's 44871 can also
be heard propelling the demonstration freight into the headshunt much
to the chagrin of photographers on the bank waiting to photograph 957's
departure!
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957 departing from Keighley |
2:56
1.3MB
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The railway was making maximum use of the two visiting Black 5s and
it was 44871 that took the next train out of Keighley for Oxenhope.
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44871 departing from Keighley |
3:52
1.8MB
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The demonstration freight was next having a short run to Ingrow and
back.
957 had nine wagons and a brake van behind the tender but, at the rear
was 47279.
Banking passenger trains on the K&WVR isn't allowed but no such
restriction applies to goods trains so the Jinty can be heard giving
the train a good healthy shove!
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957 banked by 47279 on freight
departing from Keighley |
3:15
1.5MB
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My original intention, after recording these four trains had been to
catch the next train up to Oakworth but having studied the timetable
I soon realised that I would only be able to make two recordings up
there before I'd have to return to Keighley and I would miss the chance
to record the Jinty again so I decided to stay down at Keighley. For
a bit of variety, I moved up the line to try a few recordings on G.
N. Straight which I also thought would be a bit quieter than the area
around the station.
The next train out of Keighley due off at 12:45, was to be double headed
by 44767 piloting the WD 2-8-0 90733 and as the pair departed from Keighley
station about half a mile away, the Parish Church clock can be heard
chiming the hour; as often happens at galas, trains were not quite running
to schedule!
As you can hear, most of the work was being done by the Black 5; the
WD was just chuffing gently.
The next train should have been a shuttle to Ingrow with 957 but due
to late running this never appeared; they dropped it from the timetable
in an attempt to make up a little time; the attempt failed and late
running continued for the rest of the day.
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44767 & 90733 on G. N. Straight |
3:04
1.4MB
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I'd hoped that G. N. Straight would be quieter than the area round
Keighley station and, for a while it did seem to be but as 44871 departed
from Keighley someone at an engineering firm at the other side of the
river decided that now would be a good time to begin banging a large
piece of metal with a big hammer.
Fortunately the banging stopped before 44871 passed but it seems that
the hammer wielder had only laid his hammer aside so that he could go
and get his angle grinder!
Of course, once 44871 was well and truly out of earshot, the noise stopped.
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44871 on G. N. Straight |
2:49
1.2MB
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Next was one of the reasons why I'd stayed at the Keighley end of the
line. According to the timetable the next train was a shuttle to Ingrow
hauled by the Jinty by itself although, when the train with 47279 at
the front appeared, the two coaches had the addition of 957 on the rear.
No doubt this was in the hope of speeding up the turn round at Ingrow
as trains were still running rather late.
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47279 on G. N. Straight |
2:08
1.0MB
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Most gala days feature a non-stop run of some kind but now that the
railway has decided that these trains should at Haworth, they are marked
in the timetable as 'Express' and that was next train off Keighley.
To be honest, I've recorded these trains quite a few times over the
years and have to say that, understandably on a short branch line where
the maximum permitted speed is 25 mph (in theory at least!) and while
they do their best, of course, it's quite hard to run a convincing express.
There was one train back in 2006 with 80002 that was pretty impressive
passing Oakworth but generally, these trains haven't lived up to my
idea of an express.
Still, even if it doesn't sound exactly express, 44767 sounds pretty
good passing on G. N. Straight.
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44767 on G. N. Straight |
2:49
1.2MB
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After that I returned to the environs of Keighley station where I hoped
that, it being Friday afternoon the workers at the builder's merchant,
etc., might have knocked off early! Sadly, the concept of POETS day
seems not to have reached them so I took up my position behind the wall
again.
Another feature that seems to have become a regular thing at galas
is the running of a triple header; not something that I am at all keen
on. Double headers can be bad enough but three is too much for me.
The next train away from Keighley was the day's triple header but wouldn't
get its third loco until it reached Ingrow where 957 would be attached,
the other two locos being 90733 piloted by 47279.
I was pleased to hear the Jinty doing at least its fair share of the
work with this 6 coach train.
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47279 & 90733 departing from
Keighley |
2:41
1.2MB
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For my last recording I was delighted to see that both the builder's
merchant and the warehouse behind me had both shut up shop for the day
so I was able to go to my preferred recording spot at the top of the
embankment at the other side of the line for a final recording of 44767.
The big advantage of this location is that you can hear the full effect
of the echoes from the surrounding buildings as 44767 departs.
Once 44767 had departed, the other Black 5, 44871 can be heard coming
out of the station and into the headshunt to collect a couple of extra
coaches for the next train.
Two Black 5s for the price of one; not a bad way to end the day!
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44767 departing from Keighley |
4:33
2.0MB
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An old friend
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Added 15th Dec 2010
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 In
early December I found myself with a couple of hours to spare in York
and naturally spent them in the National Railway Museum. Reaching the
turntable in the main hall I was most surprised to run into an old friend
that I hadn't seen in ages; none other than 'Maude'. I'm referring to
the loco of that name, of course, rather than a lady friend!
'Maude', having served in France during the first world war was named
after the general of the same name rather than a lady and looked a bit
different to the way the loco used to look when I travelled behind it
back in the 1980s. Then the loco carried the number 673 and North British
Railway livery as a Class C Goods 0-6-0 but there on the turntable,
looking very smart, 'Maude' had returned to BR black livery carrying
the number 65243 as a J36 which was how I first saw the loco on Bathgate
shed back in the 60s; an old friend indeed!
In the 1980s the Scottish Railway Preservation Society regularly made
use of the loco on railtours from their Falkirk base and days out with
'Maude' could always be guaranteed to be entertaining...
My first outing with 'Maude' was on 15th October 1983 when this 1891
veteran worked a four coach train from Falkirk to Perth and back out
via Stirling and back via the Forth Bridge.
During most of the day the loco never seemed to be steaming well but
we did get to Perth without any unnecessary stops to regain boiler pressure
or water level.
Returning from Perth via Ladybank, the final steep gradient to be climbed
was that from Inverkeithing up to the Forth Bridge and would have been
a most embarrassing part of the journey to stop short of steam!
Fortunately 673 was able to make the ascent on to the bridge without
stopping - just!
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673 climbing from Inverkeithing
to the Forth Bridge. 15th October 1983 |
6:32
3.0MB
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On another similar run in 1986 we went round the same circuit, but
in the opposite direction and things didn't go quite so well...
On 20th September 1986 the Scottish Railway Preservation Society celebrated
its 25th anniversary by running a railtour, The Silver Jubilee, to Perth
with 'Maude'.
Soon after leaving Falkirk, as 'Maude' with just 4 coaches behind the
tender plodded up the climb to Polmont we soon began to realise that
the loco was not steaming well and having reached easier gradients on
the Glasgow - Edinburgh main line the loco was obviously struggling
to maintain a reasonable pace.
Reaching Linlithgow we were put into the loop while a few trains overtook
us and this gave the loco crew the chance to attempt to get some life
into the fire and, after some time and with a decent pressure in the
boiler, we departed from the loop, reached Winchburgh Jc. and continued
to Dalmeny joining the main line from Edinburgh to Dundee before setting
off across the Forth Bridge.
On the approach to the bridge we came to a stop while boiler pressure
was regained. After a short wait we were able to proceed but all was
far from well and we eventually came to a stand almost in the middle
of the bridge.
The
loco was unable to regain pressure and, in due course, a following loco
hauled service train was brought up behind and pushed us to Inverkeithing
where we were able to get off the main line and allow a number of trains
that we had delayed to overtake.
The decision had already been taken to provide us with a diesel pilot
which would assist as far as Ladybank, where we were booked to take
water but from there we would be on our own again.
We did eventually reach Perth where the loco's support crew were able
to discover that the problem was located in the loco's smokebox where
the blower ring had become detached. This meant that, not only did the
blower not work, but the detached part had been affecting the blast
through the chimney, reducing the draft through the fire and 'Maude's
ability to make steam.
Repairs were soon made but as we were rather late departing from Perth
it came as something of a surprise when we still made our booked photos
stop at Gleneagles.
The top of the climb from Perth isn't far beyond Gleneagles and 'Maude'
makes a fine sound departing and reaching the summit.
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673 departing from Gleneagles.
20th September 1986 |
2:37
1.2MB
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Back in 1984 steam hauled trains returned to the West Highland line
between Fort William and Mallaig. Over the Spring Bank Holiday Weekend,
as a prelude to this first year of regular steam operation on the route,
S.L.O.A. had arranged a three day visit based on Fort William to include
the first public trains. Looking back it seems remarkable that the total
cost of this weekend, including three steam hauled runs on the West
Highland Extension and two nights dinner, bed and breakfast was just
£67.50!
Despite the continuing fine weather and high fire risk Bernard Staite
assured us that everything would be Ok and the trains would run. He
was proved right, but it wasn't as straightforward as that!
The first public tr ain
(there had been a press run during the previous week), hauled by 5407
left Fort William at 9.00 am on Sunday 27th May 1984 and after a run
to Mallaig and back, the original intention had been to use 'Maude'
on just 4 coaches for an afternoon run to Mallaig and back. Half the
passengers would travel on the train one way while the other half travelled
by bus to get some lineside photographs with passengers swapping over
at Mallaig.
There had been some doubt over 'Maude' reaching Fort William because
of shortage of coal supplies due to the continuing miners strike and
while the engine had made it, it had run a bearing hot during the journey
north so was not available and 5407 did the honours once more.
Those of us with accommodation in the Milton Hotel, which is quite close
to Fort William depot, could have got up in the early hours to view
'Maude' being driven gently up and down the yard had we so wished. The
SRPS support crew had burnt the midnight oil re-metalling the offending
axlebox and then gently bedding it in. The result of this effort was
that 'Maude' was available to run to Mallaig on the Monday morning.
The stock used was part of the S.L.O.A. first class set which had brought
us up from the south as the B.R. stock which we had used the previous
day was required for the public steam hauled train later that day.
So, with just 4 coaches it was a short but very well filled train that
left Fort William for Mallaig at 8.30 am on 28th May 1984.
Although I said above that the train was going to Mallaig this wasn't
exactly the case. While the intention was to go to Mallaig there were
no guarantees that we would get there. If things didn't go well we could
expect to be turned back earlier.
However, in the early stages of the run, after a short pause at Banavie,
'Maude' sounds to be going well rattling over the swing bridge across
the Caledonian Canal and tackling the rising gradient beyond.
So far so good.
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673 passing Banavie. 28th May 1984 |
1:58
930KB
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As far as Glenfinnan, things went Ok. We had a stop there to check
on the state of the bearing and add a little water to the tender but
when we left we were rather late compared with the intended timings
which, of course, were for a Black 5! Despite the late running we still
had the booked photo stop at Lochailort where the loco performed run
pasts.
The next serious climb was Beasdale Bank which had caused 5407 to stall
on the first run the previous day.
While not fast 'Maude' sounded to be coping with the load on the climb
until we passed through the top tunnel onto the curve beyond where speed
began to fall rapidly and the loco began to slip a little.
After that the rest of the climb turned into something of a stagger!
As you can hear in this recording, in due course, 'Maude' made it.
We continued to Arisaig where the decision to turn back was taken. For
all the time that it saved we might as well have continued to Mallaig!
Running round at Arisaig was no easy matter and there was no water available
which the loco now badly needed.
The return journey was full of incident too.
We stopped alongside Loch Dubh, between Beasdale and Lochailort and
took water from the Loch! It could have been shades of 'Titfield Thunderbolt'
but for a handy diesel pump.
As well as starting a number of lineside fires we stopped for a blow
up on the climb from Loch Eilt and eventually arrived back at Fort William
extremely late having thrown the West Highland Line into total chaos.
And the S.L.O.A. train still had to get back to London!
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673 on Beasdale Bank. |
2:38
1.2MB
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On
1st December 1984 the SRPS ran a most interesting tour with 'Maude'.
The train, named the Suburban Centenarian, was to celebrate the centenary
of the Edinburgh Suburban line but the route of the tour also took in
most of the Edinburgh - Glasgow main line.
We left Falkirk heading west and having passed under the Edinburgh -
Glasgow main line 'Maude' had to tackle the rising gradient from Castlecary
towards Cumbernauld. On the 1 in 98 gradient, although speed fell the
loco sounded to be doing Ok but approaching Cumbernauld, although the
gradients had eased a little it soon became apparent that all was not
as it should be and eventually the sound of dragging brakes could be
heard as the boiler pressure fells lower. The end result was never in
any doubt.
A blow up was the order of the day and, with the boiler pressure at
a more respectable level 'Maude' restarted the train and continued on
the climb to pass Cumbernauld station which marks the summit where this
recording begins.
The driver decides to take full advantage of the falling gradients beyond
and allows the loco to reach our top speed for the day, 45 mph. Not
bad for a loco restricted to 35!
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673 passing Cumbernauld. 1st December
1984 |
2:28
1.1MB
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Our route from Cumbernauld took us to Springburn where we stopped for
water, some attention to the loco (perhaps 45 mph wasn't such a good
idea) and, if memory serves, for some Civic dignitaries to join the
train. Then with water taken and guests on board we departed and soon
joined the Glasgow to Edinburgh main line. Pathing 'Maude', maximum
speed 35 mph, on the main line can't have been easy and it will come
as no surprise to hear that we visited almost every loop between Cowlairs
and Edinburgh to allow other faster trains to overtake.
When we eventually reached the outskirts of Edinburgh, instead of running
straight into Waverley station we were routed around the Edinburgh Suburban
line the Centenary of which was the whole point of running the train.
The climb up from Haymarket is steep, eventually reaching 1 in 70 before
reaching the summit of the line at Morningside Road. Adhesion wasn't
too good and 'Maude' had a bit of a struggle but, as you can hear in
this recording, we did make it.
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673 climbing to Morningside Road. |
2:45
1.2MB
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Running trains round the Edinburgh Suburban line in the weeks leading
up to Christmas became something of an SRPS institution and with Santa
on board, were always very popular and well filled. There was always
plenty of entertainment involved and after that first time in 1984 I
made a point of having a weekend in Edinburgh each Christmas for a dozen
or so rides round the Sub with Santa! Of course, travelling 12 times
during the weekend meant that there were 12 opportunities to tell Santa
what I wanted for Christmas. I recall asking for a steam hauled run
south from Forth William on one occasion, something that, at the time
seemed most unlikely and that eventually happened so perhaps there really
is a Santa Claus!
'Maude' wasn't motive power every year but appeared on these trains
in 1986 and to avoid the steep and difficult climb to Morningside Road
from Haymarket we went the other way round. In that direction, the climb
is longer but generally less steep and, in this recording, 'Maude' is
heard passing Niddrie West Jc. after the climb from Portobello.
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673 passing Niddrie West Jc. 13th
December 1986 |
3:15
1.5MB
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A good 15 minutes after the previous track ended 'Maude' has finally
reached the final steeper gradient to the summit of the line at Morningside
Road.
It's a shame that these trains no longer run. Do you know, I really
miss riding round the Edinburgh Sub a dozen or more times in a weekend
with Santa and 'Maude'!
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673 passing Morningside Road. |
3:07
1.4MB
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York at Christmas
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Added 26th Dec 2010
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York
was a busy place on Saturday 18th December 2010.
Of course, the railway at York is always a busy place but in the run
up to Christmas each year, York sees more than its fair share of charter
trains and on this particular Saturday there were two steam hauled trains
which were booked to depart within half an hour of each other.
The first of these was a charter from London to Newcastle which had
been hauled north by 60007 before returning diesel hauled to York where
another ex LNER A4 Pacific, 60019 'Bittern', was to take over for the
run back to London.
At Dringhouses, about a mile from the station, on this very cold but
still evening, sound was carrying very well and the A4 can be heard
begining to get its 12 coach train on the move as it passes under Holgate
Bridge.
As it approaches the A4's whistle is answered by the loco on the other
steam hauled charter train to visit York that day, GWR Castle 4-6-0
5043 'Earl of Mount Edgcumbe', which was standing with the ECS of its
train in Holgate sidings.
The A4's safety valves lift and, for a while we thought that all we
would hear as it passed was the sound of escaping steam but fortunately
the valves close.
As you can hear, there was a Class 47 diesel attached at the rear of
the train and, although it doesn't sound to be pushing when it passes,
I couldn't help wondering if it had provided a little initial assistance
as the acceleration seemed quite fast for a 12 coach load with the addition
of the diesel and the A4's second tender.
Almost as soon as the sound of the A4 has faded away, 5043 begins to
draw its train down to the outlet on to the main line as getting from
Holgate to York station requires a reversal, there being no direct access
from the sidings to the station.
The Castle has to wait for service trains to pass before getting the
road but the pause gave us the chance to record a fine example of the
sound of that unique GW blower!
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60019 passing Dringhouses &
5043 drawing ECS out of Holgate sidings. 18th December 2010 |
7:21
3.3MB
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Once
the Castle had propelled the coaches back into the station, it wasn't
long before it departed for the return journey to Tyseley.
Unlike the A4, 5043 could clearly be heard starting its train and if
the acceleration sounds rapid this time, it's all steam as there's no
diesel on the back of this train.
Approaching, the Castle slips violently but this is soon controlled
and the driver soon has the regulator wide open again.
What a fine sound.
And the rockets errupting from the chimney were pretty spectacular too!
5043 soon passes under the first of bridges to the south and the sound
fades away.
A fine recording to end the year.
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5043 departing from York and passing
Dringhouses. |
3:23
1.5MB
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Unfortunately there's a very sad postcript
to these recordings.
Checking my email when I returned home I spotted a message that the first
train we had recorded had terminated at Stevenage as the fireman on Bittern
had been taken ill. It was the following morning that I heard that the
fireman, Paul Kane, had collapsed on the footplate approaching Stevenage
and couldn't be revived.
In the 1980s when steam hauled trains returned to the S&C he was a
fireman at Carlisle and was involved in some of the epic performances
over that route that I remember so well. In the 1990s he was passed out
to drive steam locos, later joing the West Coast Railway Company and becoming
a familiar figure on their charters and particularly on that company's
trains on the West Highland line.
He will be missed. |
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It's been a while...
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Added 15th Dec 2010
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It's
been a while but on 21st November 2010 I had the chance to have a ride
on the Severn Valley Railway, somemething I haven't done for too many
years.
The railway was only open as far as Highley as work was being done on
the line north of there. Two steam locos plus a DMU were handling services
and the first train we were able to ride on was hauled by the GWR Manor
4-6-0 7802 'Bradley Manor'; this was the railway's lunch time 8 coach
diner.
At Highley we intended to visit the Engine House, the new building there
which doubles up as a museum and a place to store and display out of
service locos. I can't really comment on how good or bad the Engine
House is other than to say that, seen from the outside it looks very
smart but perhaps a bit too modern in that particular location. The
reason why we didn't go in was, having bought through tickets from elsewhere
in the West Midlands which are advertised as being valid in the same
way as SVR day tickets (which allow free entry) on trying to get in
we were told in no uncertain terms that we would have to pay. On questioning
this the lady on the till seemed to take great delight in telling us
that she had it in writing and showing us the bit of paper in question!
Since we didn't feel like paying a fiver for what would have been a
fairly short visit we didn't bother. What was even more suprising was
that although there is a shop and cafe, to get access to either you
appear to have to pay. I would have quite liked to have used the cafe
but I certainly wouldn't want to pay £5 to go and spend money
in it!
Still, never mind as the approach to the Engine House provided a convenient
location for this lineside recording of 7802 departing on its return
journey to Kidderminster.
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7802 departing from Highley. 21st
November 2010 |
1:49
854KB
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Despite
the minor disappointment of not getting to have a look at the Engine
House I have to say that I thoroughly enjoyed my ride. The trains were
busy, but not too busy; most of the rolling stock seemed to be GW vintage
compartment coaches and most comfortable and best of all, well warmed
through with good old fashioned steam heat! This later feature was most
welcome on this cold day and something that other railways that I've
travelled on seem to find difficult.
Having enjoyed one run to Highley we returned with the other loco working
trains that day, Prairie Tank 4566 before having another run later in
the afternoon from Kidderminster to Highley and back behind 7802 with
its 8 coach train and, once again, it sounded fine departing from Bewdley
heading north. The recording ends after the loco has slowed for the
level crossing at Northwood Halt before accelerating towards Arley,
the next station.
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7802 departing from Bewdley. |
7:52
3.6MB
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End of the season NYMR
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Added 4th Dec 2010
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With the end of the NYMR daily running season fast approaching, on 25th
October 2010 I paid the railway a visit just to have a ride rather than
spend the day at the lineside making recordings as I usually do but,
towards the end of the day I did make one recording at Esk Valley.
This was of the ex LNER A4 Pacific 60007 'Sir Nigel Gresley' which had
been out of service for most of the year being retubed and had only
recently returned to service.
At the head of 6 coaches the A4 sounds to be back in fine fettle as
it starts on the gradient to Goathland.
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60007 passing
Esk Valley. 25th October 2010 |
3:52
1.8MB
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I
was back at the NYMR a little over a week later on 6th November 2010,
this time with a friend from Australia who seemed to have brought some
fine weather with him; while it was cold, there was plenty of sun and,
more importantly, almost no wind. There were only two trains out on
the line that day and after a couple of recordings at the north end
of the line (and a bacon sandwich at Grosmont station!) we headed off
to Levisham for a couple more recordings.
I wouldn't want to suggest that our visit to the NYMR was centred around
the railway's catering facilities but part of the reason for going to
Levisham was knowing that we would have plenty of time to get a drink
and a piece of cake at the Weighbridge tea hut which is always well
worth supporting!
Suitably refreshed we headed off into Newtondale to record 45212 returning
from Pickering and in the very calm conditions set up our equipment
near Gallock Hill, not far from Kale Pot Hole.
Sound wasn't carrying well enough for us to hear 45212 departing from
Levisham but we didn't have any complaints about this recording especially
as the sound carried back better than usual and we must have been able
to hear the train almost all the way up to Newtondale Halt.
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45212 at Gallock
Hill. 6th November 2010 |
5:15
2.4MB
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For our last recording of the day (after another visit to the Weighbridge
for more refreshments!) we tried a spot opposite Yorfall wood.
Once again we didn't hear 76079, the other loco out that day, leave
Levisham but again sound did carry back for a long time and the sight
of the trail of steam hanging in the still air all the way down the
valley in the dusk was really something to see!
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76079 at Yorfall. |
4:27
2.0MB
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The best laid schemes
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Added 4th Dec 2010
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On the following day my Australian friend and I had some steam on the
main line to go out for and I had carefully planned an itinerary for
us which should have allowed us to have a chance of getting four recordings,
three of them on some of the steepest gradients around and without needing
a desperately early start.
The train we were out to record was the interestingly named Tin Bath
Extra hauled by both of Ian Riley's Black 5s, 45407 & 44871. This
was to run from Preston to Manchester then through the Hope Valley to
Sheffield. From Sheffield it was routed up the steep line to Penistone
and Huddersfield then via the Calder Valley to Copy Pit returning to
Manchester via Blackburn and Sough; an excellent itinerary for some
good lineside sound recordings.
Robert Burns wrote that the best laid schemes of mice and men gang aft
agley and, shortly before we set off for the Hope Valley news reached
us that the line was blocked by a derailment! Rumour had it that the
train was going to run but be re-routed between Manchester and Sheffield
via the WCML and Derby which, if true, was going to mean some very late
running.
Despite the uncertainty we set off in the general direction of Sheffield
and, while on the way, had confirmation from someone at WCRC of the
altered route to Sheffield but doubted his expectation that the train
would be not far off regaining its booked path at Sheffield. My guess
was that it would be at least an hour late, probably more.
As my original plan of going to Hathersage had to change so instead
we headed south of Sheffield to try to get a recording on the climb
through Dronfield to Bradway Tunnel.
I had identified a possible spot on the map at Unstone not far south
of Dronfield so we headed there and the spot proved to be Ok, a little
too close to a road but as there didn't seem to be anywhere better we
settled down to wait for some more information about the train.
Eventually news reached us that the train had left Derby but it was
around 3 o'clock before it passed our spot going very well on the 1
in 100 gradient but over an hour after it should have left Sheffield!
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These two images are stills from a video taken by my Australian friend.
To see the full video, visit
Youtube and you can hear his recordings at Steamsounds
AU
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45407 & 44871
passing Unstone. 7th November 2010 |
1:58
928KB
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When we set off for our next location we still weren't sure if the
train would now go via its booked route through Barnsley and Penistone
to Huddersfield as pathing an out of course train on this mainly single
track route could be difficult and the people at Network Rail could
easily have sent it via a less difficult route. However, while on our
way we got the information that the train would be leaving Sheffield
at 15:50 and would go via Penistone so we continued to our planned location
at Summer Lane on the steep climb from Barnsley.
This area is heavily built up and there are plenty of busy roads around
so, while conditions were good; it was dry and there was almost no wind,
traffic noise was a bit of a problem.
A little later than expected we heard the two Black 5s coming up the
1 in 50 gradient from Barnsley and, after a slip near the site of Summer
Lane station, recovering some speed as the line becomes straighter and
the gradient eases slightly to 1 in 57.
It's not unusual for double headed trains involving two locos of the
same class to not sound like a double header as the tow loco's
exhaust beats often synchronise but in this case, perhaps partly due
to the difference in thickness of the two loco's tyres (45407's tyres
are near to scrapping thickness apparently), we could hear both locos
clearly as they passed going very well with this 11 coach train.
After this, though we already knew that the run over Copy Pit and Sough
had been abandoned with the train returning direct to Manchester via
the Calder Valley there was still a booked water stop at Brighouse so
we headed there in the hope of getting a recording of the pair departing.
The train did stop at Brighouse but it was only a brief one as no water
was taken so we missed the chance of a recording. Still, even if we
didn't get the four recordings we expected, we managed to get something
and at least the train did run!
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45407 & 44871
near Summer Lane, Barnsley |
2:55
1.3MB
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At Last!
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Added 4th Nov 2010
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Locos
of the Great Western Railway and lines in the North of England in the
past haven't mixed all that well and, generally speaking, have been
a great disappointment to their supporters, even the fanatical ones.
Now, it's a well known fact that I have a fairly low regard for the
products of Swindon and my opinion remains that, while the GWR did have
some of the best locomotive designs in the world in the 1920s and 30s,
that development didn't continue. It was almost as though they were
saying, 'Now we have the best, we don't have to improve anymore.'. Fortunately,
other railways didn't have the same outlook and I have always been very
glad that William Stanier managed to escape in time...
Back in 1985 during GW 150, amongst all the disasters, there was one
loco that did well on the trains that it worked and that was 'Clun Castle'
which proved far more capable than other locos of the same class thanks
to improvements made by BR on the basic 1920s design and although Clun
is not currently a runner, the appearance of another 'improved' Castle,
5043 'Earl of Mount Edgcumbe', on the main line gave hope for some better
performances than others of the same class had produced in the north.
On 16th October 2010 5043 was to work a train over the Settle to Carlisle
line, the route that other Swindon locos had come to grief on and I
felt that the title of the train, 'The Pride of Swindon' was asking
for trouble; well, we all know what pride comes before...
In this instance, pride did not precede a fall and the loco performed
well with its train of 10 coaches with the addition of a Class 47 diesel
attached at the rear no doubt added for insurance, just in case, and
of course to fuel speculation about did it or didn't it push. Reliable,
as well as unreliable, sources say it did push northbound but not southbound.
Having
had a look at the loco at Hellifield we went to Helwith Bridge for our
first recording and, when we got there with plenty of time to spare,
conditions seemed excellent with only a light breeze from the north
east. Of course, by the time we set up our equipment on the hillside
which backs on to the quarry the breeze had strengthened somewhat; isn't
it always the way?
The Castle was due off Hellifield at 10:45, following behind the 09:47
service train from Leeds so we knew that a DMU would pass first but
we never saw it and, while we were still expecting the service train,
to our surprise, steam appeared down towards Stainforth.
From our spot it was impossible to tell if the diesel was providing
any assistance but 5043 seemed to be doing very well coming up the 1
in 100 gradient and accelerated nicely on the short level section below
our microphones. Having passed, the wind carried sound back well and
we muct have still been hearing the Castle well above Horton - in -
Ribblesdale.
Not a bad recording, 5043 was just as noisy as expected and so far,
so good.
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5043 passing
Helwith Bridge. 16th October 2010 |
3:57
1.8MB
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For the southbound run to Ais Gill, as the wind didn't seem too strong
we decided to try a recording not far from the summit, a spot that we
hadn't recorded at for some time.
Once again the wind was in the right direction to carry the sound to
us and this time we were able to hear 5043 for some time before it appeared
round the curve from Mallerstang.
As with the northbound run, the Castle, although needing to be worked
very hard, seemed to be doing well on the climb.
Despite the wind being from the wrong direction we could hear 5043 for
some time after it had passed the summit.
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5043 passing
Ais Gill. |
4:03
1.8MB
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After a fast run via the M6 we just had time to get to Langho on Whalley
Bank for a final recording.
This spot has the disadvantage of being between too busy roads which,
although some distance away, are still quite noisy. In addition we had
the occasional sound of something mechanical working at a farm behind
us but none of these noises were too annoying.
Running just about on time we were able to spot a trail of steam in
the distance as the Castle left Clitheroe soon after a service train
but it then suffered signal checks almost to the foot of the gradient
and we could just hear it recovering from a final one.
Some minutes later when 5043 passed our spot it was going well enough
but perhaps not being worked as hard as on previous recordings and,
this time, I can be fairly sure that the Class 47 was doing a little
more than just shifting it's own weight as I was close enough to observe
that the diesel's buffers were firmly in contact with the train.
So, at last, after numerous attempts over the years a GW designed loco
has finally managed a successful run over the Settle to Carlisle line.
Spurred on by this success, I wonder if they'd like to try it with an
original, unimproved loco again?
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5043 passing
Langho on Whalley Bank. |
4:27
2.0MB
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K&WVR Autumn Steam Gala
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Added 18th Oct 2010
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After
the rather disappointing gala on the NYMR, a week later there was another
gala to visit. This one was on the Keighley & Worth Valley Railway
and had a very interesting visiting loco which I didnt want to
miss. This was the BR Standard Class 5 4-6-0 73129. Ive always
had a soft spot for these locos, especially the Caprotti valve gear
versions which have a particularly sharp beat.
I visited on the first day, Friday 8th October 2010 as if everything
went according to plan, 73129 would have 4 trips up the branch by itself
as well as one double headed run.
This time I couldnt get to Keighley in time for the first train
up the branch so had to be satisfied with recording there for the first
few train, the first of these being the demonstration freight which
was hauled by the BR Standard Class 4 2-6-4T 80002 hauling a train of
13 wagons.
On a normal working day, the area around Keighley station can be a noisy
place and as well as vehicles using the nearby builders yard there was
also a rather loud fork lift operating. Nothing to be done about this
sort of thing of course but it did mean that I was unable to use my
preferred spot and had to hide the microphone behind a wall to minimize
the noises off.
Even with a few extraneous sounds, the Standard Tank doesnt sound
at all bad lifting its train out of the station.
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80002 departing
from Keighley on freight. 8th October 2010 |
3:23
1.5MB
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The next departure was the important one as it was hauled by 73129
which had been delivered to the railway boiler first into Keighley much
to the disgust of lineside photographers!
Its been a long time since I heard a Caprotti Standard Five, or
indeed any Standard Five worked hard and Id forgotten just how
loud they can be but 73129 working tender first out of Keighley with
6 coaches soon reminded me just what a superb sound they make.
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73129 departing
from Keighley |
5:22
2.4MB
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After that I caught a train up to Oakworth and headed for my usual
favourite spot down towards the loop to record 73129 double heading
with the WD 2-8-0 90733.
Here I found I had a problem. The day had become quite breezy and although
I could find shelter for my microphone, there was nothing I could do
to avoid the sound of wind in the trees which was very loud at times.
However, the wind was blowing from the right direction to carry sound
up the valley and Icould just hear the train departing from Ingrow and
entering the tunnel.
Once out again the sound, mainly of 73129, could be head all the way
up to Damems and into the loop there to await the train hauled by 80002
coming down from Oxenhope.
With the Keighley bound train out of the way 90733 leading 73129 soon
get away and head for Oakworth.
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90733 & 73129
at Damems Loop. |
2:28
1.1MB
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After that recording I decided that I didnt want to spend any
more time recording the trees so I moved to nearer to Oakworth station
where there were fewer trees although this meant that I didnt
hear approaching trains all the way from Ingrow.
While waiting to record 80002 coming back up the branch I was somewhat
alarmed to see that, when 90733 returned, it was by itself. 73129 should
have come down too as it was booked to return up the branch on an express,
first stop Haworth. What had gone wrong? Surely it hadnt failed.
As I couldnt get any information where I was it was just a case
of wait and see so I settled down to record 80002 coming back up and,
as usual, making a fine sound with its 6 coach train arriving at Oakworth.
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80002 arriving
at and departing from Oakworth |
2:38
1.2MB
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So, instead of the Standard 5, the express was hauled by 90733, not
a class of loco that would often work a passenger train, let alone an
express!
Not that Im complaining too much as it sounds fine on the gradient
climbing up from the loop.
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90733 passing
Oakworth non-stop. |
2:20
1.0MB
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By this time a friend had arrived on the railway, also making sound
recordings and was down at Keighley. Thanks to our mobile phones
we were able to find out that 73129 had a small, at that time unspecified
problem that was being fixed and was expected back in service shortly.
Good news which was soon confirmed when it returned double heading the
WD when it returned from Oxenhope.
The problem proved to be a steam leak from one cylinder, Id heard
a slight blow from the loco when it passed earlier and fortunately this
was soon fixed.
73129 even manages to make a little noise for me departing downhill
from Oakworth.
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73129 & 90733
departing from Oakworth. |
1:19
619KB
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After making another recording of 80002, next was the loco that is
fast becoming a favourite noise maker; 73129!
Doesnt it sound good climbing up to Oakworth?
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73129 arriving
at Oakworth. |
4:17
1.9MB
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After that I had one more recording to make back down at Keighley and
after a ride back down behind 73129 I met up with my friend who was
just as impressed with the Standard Five as I had been and got set up
for a final recording of it leaving Keighley.
After 6 oclock, Keighley had become much quieter so I was able
to set up in a better spot and was very pleased to get this last recording
of 73129 which sounds even better than it did when I recorded it here
in the morning.
I hope that this loco visits a few more hilly railways, the NYMR for
example, as Id like many more opportunities to record this fine
sound.
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73129 departing
from Keighley. |
4:53
2:2MB
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Past recordings available here
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